Friday, November 27, 2015

We're Afloat!




Yesterday, we were dropped into the water just before noon, with little trouble and little fanfare.

This weblog is mostly a technical report of our little trials in getting our systems running.

Our first chore when getting on the boat in the yard was to top up the batteries:  Six Trojan 100 amp-hour 12 V batteries; and to set up the solar panels and controllers to equalize them.  However, we have noticed that, as the batteries get older, the batteries bubble at lower and lower voltages.  This year, they seem to be bubbling at 13 V, and do not seem to get much higher in voltage than that. 

While the batteries bubbled, we cleaned the deck, and put the mainsail back on.  A full battened sail takes a few hours to get it reconnected, re-lace the reefing system and get her back in the lazy jacks and sailbag.  Other chores followed in the coming days:  Renovate and grease the toilet (RM 69), re-assemble the engine belts and seawater pumps, re-assemble the folding propellers and anodes, put the jib on, re-assemble the watermaker, test the electronics, test the air-cooled fridge unit, re-assemble dinghy and motor, wash and wax, and carry out various work that needs to be done on the hard.

Most things worked out o.k., just the usual time, hot work, and minor blood-letting.  However, some things were not adding up - the ham radio was cutting out, the frig would shudder but not start, the stereo sounded funny.  I was most suspicious of my batteries, thinking that they no longer had enough "depth" in their storage.  It was not until yesterday, after we anchored, that I started working on all aspects I could think of for the refrigerator.  I was tracing the negative lines through switches and fuses when I found a major negative battery switch that I had missed turning on.  Now most things are working, especially the refrigerator.

After getting the fridge to work, it was time to travel to Customs to get a new cruising permit.  We dropped the dinghy, with the motor that had successfully started on the hard, and no, it would not start at all.  I spent about 40 minutes trying spark plugs and pulling the cord with no luck.  We tried our best to row upwind to Customs, and just as my arms were going to fall off, another boater gave us a tow.  Customs was uneventful, and, as the wind blew us back towards the boat, I continued to work on the engine.  Well, the "varnish" that was likely causing the trouble in the carburetor must have started to dissolve, because it started a few hundred feet before we were home.

The other big thing that had to be done was to track down the sources of the leaks in each hull.  The watermaker inlet screen continues to leak, and will be attacked over the weekend.  The toilet seems to be the other source, and by tightening all the screws a little, I managed to strip the plastic threads in one spot and crack the plastic in another.  I've reassembled it with a lot of calking and used a pipe clamp to maintain the seal on another spot.  The toilet, an RM 69, is a Dutch product, and the spares are only available in the French chandleries.  I am searching down suppliers who might send some parts to us.  The other outstanding issue that comes to mind is the radar that has started blowing fuses for some reason.

I should report that while we were in the boatyard, we got together with John and Alex of Free Spirit for two great nights of food and drink before they headed north.  It was good to see them, but sad in that we may not catch them again before they sail back to the UK.

Today we walked about an hour to a mall, and hauled some major groceries back by bus.  We hope to leave the work alone for a few hours and de-stress. The weblog is courtesy of a free signal from the boatyard that surprisingly we can get from the boat.